have a couple logs to show good af's at wot. Sled was broken in on the trails last march, very easy just like they want. Put turbo on this summer, made a test run or two a few weeks ago when we had snow, tweaked the map and tested again. Af's looked great.
Sled ran great on a short ride Sunday, never missed a beat, probably never hit wot at all. Maybe a little boggy at .25 throttle, but cleaned up and was crisp above that. Went to ride the next day. started sled, waited til 118 on the temp and drove easy to town cracking throttle every now and then and noticed a pop, like a backfire. Looked at overflow, seemed a bit too busy for my liking, but had never looked at it before. Went on for a few more miles of ditch riding, not hard riding at all as snow was already set up. stopped in a drive way idled a few seconds temp 130 and shut off. Never started again. mag side was checked at 30 psi, it is the better looking piston. Pto side had 80 psi and looks terrible lol. Neither piston got to the second ring, so it was sill intact. Pto piston had lost some of its ring into the pipe.
Plugs look good, really too rich actually,
150 miles approx on sled, MAYBE 30 with the turbo
working with turbo kit man to see what might have caused this, but we are a bit perplexed since all signs were good.
ideas????
![pto side.jpg pto side.jpg](https://www.snowest.com/forum/data/attachments/207/207620-73fde4c682899a36a810c245e779ca3f.jpg?hash=c_3kxoKJmj)
Sled ran great on a short ride Sunday, never missed a beat, probably never hit wot at all. Maybe a little boggy at .25 throttle, but cleaned up and was crisp above that. Went to ride the next day. started sled, waited til 118 on the temp and drove easy to town cracking throttle every now and then and noticed a pop, like a backfire. Looked at overflow, seemed a bit too busy for my liking, but had never looked at it before. Went on for a few more miles of ditch riding, not hard riding at all as snow was already set up. stopped in a drive way idled a few seconds temp 130 and shut off. Never started again. mag side was checked at 30 psi, it is the better looking piston. Pto side had 80 psi and looks terrible lol. Neither piston got to the second ring, so it was sill intact. Pto piston had lost some of its ring into the pipe.
Plugs look good, really too rich actually,
150 miles approx on sled, MAYBE 30 with the turbo
working with turbo kit man to see what might have caused this, but we are a bit perplexed since all signs were good.
ideas????
![mag left pto right.jpg mag left pto right.jpg](https://www.snowest.com/forum/data/attachments/207/207593-e59bb10e8d8a29cdd2beef797bea6138.jpg?hash=5ZuxDo2KKc)
![plugs.jpg plugs.jpg](https://www.snowest.com/forum/data/attachments/207/207604-33c5a512ace22479db91a9e0d03067fc.jpg?hash=M8WlEqziJH)
![mag side.jpg mag side.jpg](https://www.snowest.com/forum/data/attachments/207/207612-ad1696584e201287f3bb3cceabd2fcac.jpg?hash=rRaWWE4gEo)
![pto side.jpg pto side.jpg](https://www.snowest.com/forum/data/attachments/207/207620-73fde4c682899a36a810c245e779ca3f.jpg?hash=c_3kxoKJmj)